OK so done a little bit of work on the car as I had some time spare.
Decided to get the return oil line sorted on the turbo as it was seeping oil.
Car as it was before I started removing parts
https://fbcdn-sphotos-h-a.akamaihd.net/hphotos-ak-ash3/164215_489911387750176_33438322_n.jpg
Intercooler and Boost pipe work now removed, here you can get to see how the V-Mount is positioned along with the ducting.
https://fbcdn-sphotos-c-a.akamaihd.net/hphotos-ak-frc1/1005783_495627680511880_2069171341_n.jpg
Started to unbolt the Turbo from the manifold, this took a little bit of time as there is pretty much no room to get to the rear bolts, in the end it took around an hour to get it off...
https://fbcdn-sphotos-a-a.akamaihd.net/hphotos-ak-ash3/935100_495627953845186_1220554282_n.jpg
One of the car with the turbo removed
https://fbcdn-sphotos-g-a.akamaihd.net/hphotos-ak-prn1/67455_495628173845164_1536580609_n.jpg
This shot shows the oil saturation on the return hose, this hose is a fireproof high temp hose so it can be reused.
https://fbcdn-sphotos-h-a.akamaihd.net/hphotos-ak-prn2/970634_495628607178454_577006095_n.jpg
Now the Turbo is on the work bench I can get a proper look at where the leak is coming from. I had always suspected the leak was coming from the flange gasket as it looked a bit moist.
https://fbcdn-sphotos-b-a.akamaihd.net/hphotos-ak-ash4/998747_495629337178381_1308516293_n.jpg
Removing the oil drain pipe showed that the gasket had failed.
https://fbcdn-sphotos-e-a.akamaihd.net/hphotos-ak-prn2/1075661_495788390495809_1782417629_n.jpg
Although taking a closer look at the gasket it showed some damage running from the center almost to the outside edge, this must have been the cause of the leak.
https://fbcdn-sphotos-g-a.akamaihd.net/hphotos-ak-ash4/1000872_495789740495674_1427744444_n.jpg
So I replaced the gasket and got the turbo reinstalled, I also added some more heat protection on the return hose just for peace of mind.
https://fbcdn-sphotos-d-a.akamaihd.net/hphotos-ak-ash3/579581_497838293624152_1682705598_n.jpg
While I was at it, I also noticed the wideband AFR sensor connector had evidence that it got a little too hot by the downpipe (was a little bit melty), therefore I decided to add some heat shielding material to the AFR connector and cable, again for peace of mind
https://fbcdn-sphotos-f-a.akamaihd.net/hphotos-ak-ash3/549463_497851690289479_864776273_n.jpg
Finally I also changed the Radiator cap with a new Whifbitz 1.1bar cap as the other one had failed.
https://fbcdn-sphotos-h-a.akamaihd.net/hphotos-ak-frc1/1005191_497863333621648_651001929_n.jpg
I then set about putting it all back together and this is how it now stands.
https://fbcdn-sphotos-b-a.akamaihd.net/hphotos-ak-prn1/995938_497871070287541_1715409837_n.jpg
I am setting about re-installing the downpipe this weekend and hope to get on with the rear upper bushes as well. I will then hopefully get to take it out on a test drive to see if the repairs and replacement parts for worn components have sorted out the vibration issues.